Got the speakers in.
Side vents in.
Door seals in.
Refined the MACE CAI as in the pic bellow. Rubber edging on lid and intake pipe and some minor filing/sanding to get the best shape on various bits.
Cavity wax in battery tray seams and underneath seam edges
Battery in
ECU in.
Uploaded a basic starting tune.
Finished fuel hoses on the tank.
Got some fuel.
Tested electrical.
Calibrated WB
Calibrated TPS min WOT voltage to suit the wider range of the 70mm TB.
Primed the oil system. Oil light goes out after half to one ref of the engine and holds over 30 sec before the light comes back on.

Good tolerances!
And then this happen
[youtube]
https://www.youtube.com/watch?v=qv6pPhWesjU[/youtube]
Only had 2 small issues, fan stopped working (see the 104c in the video), did work when I sent a command to test it before starting it but I found the terminal in the relay block vibrated out, the tang on the terminal was bend the opposite way and must of all but pushed out when installing the relays.
The other was leaking radiator cap, turns out being a trident one not a CPC one like I wanted it didn't want to go the last bit as it was really tight on the tabs, I had to put half my body weight to get it over the tabs to turn the last bit and then it was ok.
Apart from that the engine is happy. Did a el cheap stethoscope on the engine with a hose and the only sound I could hear was the injectors when probing the fuel rails, the rest of the engine it is as quite as a mouse in there.
It is really difficult to get to idle. Idles ok at low temps and at full warm (with a bit of work it did) warm/hot restart is a no go. It dies after 10-15 sec and AFRs look ok though it is hard to tell being all jumpy with the tail pipes sucking air (wasn't long enough)
Hot restart seems impossible. Just cranks and sputters here any there, tried from 10% to 200% incremental adjustments in cranking fuel with no change except at 200% it doesn't fire at all. Cold star seemed to be ok though. So perhaps it's just way out but all the tables were accurately calculated for the new injectors and it did fire up ok on the very first try.
I also tried warm restart IAC, from 65 to 150 as It does start with the throttle open without fail. idle steps were around 40 ish when at full temp. At the 150 step mark it still made no difference. It acts like there isn't enough air, cranking has some black smoke and even does with almost no cranking pulses.
Same sort of behaviour as HQ's COME manifold when we found out the IAC port was blocked off. Hmmm I should check the IAC probably, though the stall saver does work.
Idle timing has been adjusted to what seems to be most stable with stable and decent vac. Idle speed is 950 atm, it won't idle below that with stalling. Stall saver for now is 600 and only just catches it but works 7/10 times I reckon.
I got some logs of the hard start and random stall which I will post tomorrow.
Got a very basic log to get some VE dialed in, above idle it is extremely lean. I had to increase the injector rate 20% and almost out of VE as is, will probably run out again as it hasn't been dialed in yet and almost off the scale lean above idle. Idle area is ok now after the 20% extra injector rate, not perfect but well ball parked so that is a start.
Probably will need some help with the start and idle areas as I have little experience with large cams and idle. This is way more challenging than G's race engine tune wise. His was already ball park out of the gate, this is a mess lol
