Time for an update and general goings on.
$%^^#$$!@!$, Where do I start?!
Okay, during the time I was correcting the low speed timing to cure the hunting and lurching I was logging regularly.
It was also this time I noticed how having the laptop connected interrupts BCM comms, so the low speed fan doesn't work.
Not good while idling in the Maccas drive through..... Watched the temps skyrocket and the overflow to puke after I got the thing out the gate and quickly parked it... activate low speed bypass plug NOW! (Grounds the relay so fan always on with ignition)
Fark... Everything settled down and we resumed our journey.
1st question, why the hell didn't 'fan 2' ecm controlled kick in? Is there a dependency other than the 6sec delay I can see in the code?
I've almost finished setting up a VR V8 style fan on the front of the condensor activated by a temp switch from Jaycar.. I'll call it 'Fan 3 '.
Next,
I had a pool of coolant under the rear of the supercharger.. in a recess in the LIM... looks like it came through the bolt!
Also a bad mis-fire getting progressively worse under load. Right then... LIM gaskets... bought a G-Force kit, it'll do.
Whilst apart, I knocked up a little rig to test the injectors, its a bit of a jury rig, but enough to kinda see if the squirters could deliver a reasonably equal volume of fuel.
New orings and filter baskets... they tested well.
But, this brings me to question 2... I still have a horrible split between the banks. lh+3%, rh -10%.. basically.
What to try next?
I have swapped O2 sensors, and even swapped to another set.. NTN vs Bosch. No diffference.
Swapped to a different ECM ('728) for a quick test.. no difference. (Well, Worse actually.. no LTFT memory, all STFT)
The earths of both O2 sensor grounds are linked ... slight difference.
I think i even managed to inadvertently swap the injectors from one bank to the other during maintenance.... No difference.
I haven't done a compression test, or changed the head gaskets... yet.
But general driving it seems fine, other than the data-log telling me it isn't. The miss-fire is still felt at full power, so it isn't fixed.
While rooting around putting the 'charger back on, I found one of the boost solenoid hoses split at the 90* boot.
The one from the tree to the solenoid. I figured, you know what.. I'll delete the thing, since I can't get my hand behind the head to fit another hose. Simple job.
Well it turns out my solenoid was playing up anyway.. the valve is now open at idle like it should be and its a lot quieter in general. Hmmm.
But a third problem is really confusing me.
Fuel Pressure.
For the conversion, I bought a EFP-159 Delphi fuel pump. VS S/C internal pump. Perfect. About 48psi at idle.
Under boost (10psi pulley), you can briefly watch the pressure 1:1 rise to 60psi, then as the injectors open longer IT DROPS.
Yesterday I watched it fall to 38psi at WOT!
It can't feed the volume required at the required pressure. But, essentially it should. (Fuel filter is a Z168 large VK/VL style, should it be a smaller Z200)
Maybe I have to try fit an external 044 (or tre-200) and feed it with the delphi? Directly or use a swirl pot? At least this old EFI VK has a bracket for an external pump.
I won't mention the tree that tore my antenna off, or the front wheel bearing failing again, or the reverse light switch is now stuck on.
Cheers!
-sean
Edit, Attached a new log... '728 ecu fitted... 1st run. Nasty STFTs. Lean spikes?
VS_SC_$51 enhanced XDF/ADX req'd.