
spent a few hours last night getting the last bits sorted and fired her up, all testing seemed to work ok so we had some late dinner than went for a spin up the road, I wasn't too worried about the motor more so the T700 that I pretty much fully dis-assembled then re-assembled with new clutches and such, but it so far seems to be doing everything right! shifts very firm and even chirped into 2nd gear, its never done that before

time to give it a bit more, and so the brother pulls out of an intersection and laid the boot in and at 3.5 psi it blew the intercooler pipe off!! quick check on the side of the road and it looks like he did up every clamp except that one! so im thinking previous runs it was probably bleeding a fair bit of boost out the hose anyways, and it looked like it was boosting later than it used to.
so we limped it back home and by this time it was 9:30 and I still had a 1.5hr drive ahead of me, so we called it a night.
only issue we found is there is some oil coming out around the inspection cover, so we'll need to check that, its got a second hand cam plug in it and also there was some issues when my brother installed the rear main (lip folded over) so maybe one of these two are causing the leak, wont know for sure till we get under it.
either way it looks like its going to have plenty of potential!! and considering what's been done I'm very happy to only have a small oil leak
